Drag RacingFind out the best way to launch and see what kind of times other people are posting. No posting of street racing related stories!
Welcome to EvolutionM.net!
Welcome to EvolutionM.net.
You are currently viewing our forum as a guest, which gives you limited access to view most discussions and access our other features. By joining our community, at no cost, you will have access to post topics, communicate privately with other members (PM), respond to polls, upload content and access many other special features. Registration is free, fast and simple, so please join our community today!
Pat's Evo 9 runs a personal best but ...... UPDATED W/ VIDEO
Made a trip out to the track after putting in the 5point bar and switching to 1450's and E85.
Was just going to make a few passes to fine tune and log info and had some good and bad news.
I was one of the first 20 cars and the 10th car oiled down the track for an hour
Finally got to make a pass and the car left a little soft and was making a decent pass but for some reason my gutt said to lift in 4th gear
Get back to the pits and shut her down and then i see coolant coming from the front timing assembly area so i think the water pump said goodbye
The over flow was not filled and the tube itself totally dry. Car never overheated and logs showed normal coolant temps however i did have the heater blowing after the pass which i do every time possibly masking the rising temps???
The car did run a personal best (not by much lol) but does give me great hope to get the car deep into the 10's w/ a possible 9 sec pass in the near future.........
I have a vid that will be posted as well as the slip i know it's not much but it's def progress now i gotta start researching water pumps and failure and why.......if you have info on that please do share links etc.
Made a trip out to the track after putting in the 5point bar and switching to 1450's and E85.
Was just going to make a few passes to fine tune and log info and had some good and bad news.
I was one of the first 20 cars and the 10th car oiled down the track for an hour
Finally got to make a pass and the car left a little soft and was making a decent pass but for some reason my gutt said to lift in 4th gear
Get back to the pits and shut her down and then i see coolant coming from the front timing assembly area so i think the water pump said goodbye
The over flow was not filled and the tube itself totally dry. Car never overheated and logs showed normal coolant temps however i did have the heater blowing after the pass which i do every time possibly masking the rising temps???
The car did run a personal best (not by much lol) but does give me great hope to get the car deep into the 10's w/ a possible 9 sec pass in the near future.........
I have a vid that will be posted as well as the slip i know it's not much but it's def progress now i gotta start researching water pumps and failure and why.......if you have info on that please do share links etc.
congrats Patrick! you still running the qm? sorry to hear about the wp though. should be a easy fix though.
Good luck Patrick, I'm sure you will get it sorted out. It must feel good to have a safer car and not have to worry about getting the boot. Props to you for doing things the right way. BTW we bent up a six point for use at a later date . Indy
Good job man, you will get it sorted out and a full pass out of it soon.
Thanks ..............not too bad for a year and a half of racing, dynoing, and street driving everything else seems to be ok motor wise
Quote:
Originally Posted by evovin
How early did you lift?(what rpm)
Logs showed right at 6900-7000 and vehicle speed showed 130mph.......a little bench racing if you don't mind but what do you think it would have gone guys?
Quote:
Originally Posted by Indy Evo
Good luck Patrick, I'm sure you will get it sorted out. It must feel good to have a safer car and not have to worry about getting the boot. Props to you for doing things the right way. BTW we bent up a six point for use at a later date . Indy
Being strapped in tight w/ the harness sure made me feel like a real race car driver
Congrats Douglas Auto 9.97@143 first full pass | English/ETS/Jeff Bush 8.674@167 | Evosick2332/Strictly Mod 9.93@141 | M.A.P STOCK ECU HP RECORD 1053whp 721TQ | EvoDan 10.37&141MPH PRO CDI | lillev23 9.959@138.67STOCK BLOCK RECORD NON-CDI COP | [ Speedtech NZ World record 8.34@169.72 |
Innovation distinguishes between a leader and a follower.
New Product : NonCDI Sequential
The launch was so-so in my book was just trying to make a good pass and not bog or crazy spin since it was the first pass off the trailer.
It has gone 1.5x in past runs but i feel it will take a good solid 1.4x to break into the 9.99 area that's why i'm considering a switch to 24" full slicks.
Comparing to other posted slips w/ the 6.7 1/8mi i think it would have been good for 10.2x at least.